> our title:

Report: Pilot Error Caused Predator Crash

> original title:

MQ-1B Predator Accident Report Released

(Source: US Air Force; issued Oct 28, 2014)


LANGLEY AFB, Va. --- An MQ-1B Predator impacted the runway because of low-level wind shear and incorrect pilot recovery techniques during a practice landing at Creech Air Force Base, Nev., on April 4, 2014, according to an Air Combat Command abbreviated accident investigation board report released today.

The aircraft and its aircrew were assigned to the 11th Reconnaissance Squadron at Creech AFB, Nev. when the accident occurred. The aircraft was significantly damaged by the impact with a repair cost estimate of $4.5 million. There were no injuries or damage to private property. The aircrew was conducting a routine launch and recovery training mission at the time of the mishap.

The board president found by clear and convincing evidence that the cause of the mishap was low-level wind shear during a critical phase of landing, and the pilot's lack of training in landing operations for the MQ-1B. Specifically, after the aircraft experienced loss of lift due to low-level wind shear, it bounced on the runway and the mishap pilot used the wrong recovery technique for an MQ-1B.

The pilot's incorrect control inputs caused the aircraft to continue bouncing on the runway until its landing gear were destroyed.

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